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N75J let down!! Or is it!!!

Posted: Fri May 16, 2008 2:49 pm
by whitegtipolo
Received my N5J today and wat a let down , boost nearly gone down to bout 0.5 bar again doesn't kick in like it used to and hardly any dump noise!!! The valve must be faulty as it is second hand from ebay!! put my original valve back on and its bob on fast as again??? I did connect it all ok the opposite way round etc anyone else had this problem??? :( cos it really does feel alot slower with the J and you can hear the turbo not boosting as high??

Posted: Fri May 16, 2008 5:17 pm
by Jeff GTi
THATS PROBABLY IT, A DEFECTIVE PART, COULD OF HAPPENED IN TRANSIT AS THEY ARE REALLY QUITE FRAGILE INSIDE THE VALVE

I NOTICED AN IMMEDIATE DIFFERENCE PUTTING MINE ON, BOOST AND RESPONSIVENESS FELT MORE AGILE AND QUICK TO RESPOND

Posted: Fri May 16, 2008 6:11 pm
by whitegtipolo
Jeff GTi wrote:THATS PROBABLY IT, A DEFECTIVE PART, COULD OF HAPPENED IN TRANSIT AS THEY ARE REALLY QUITE FRAGILE INSIDE THE VALVE

I NOTICED AN IMMEDIATE DIFFERENCE PUTTING MINE ON, BOOST AND RESPONSIVENESS FELT MORE AGILE AND QUICK TO RESPOND
its well annoying cos i was so looking forward to it it felt unchipped couldnt hear the turbo whooshing like b4 ive sent him a message hope i get a refund was £30 :roll:

Posted: Fri May 16, 2008 7:00 pm
by MateyGuv
When I fitted mine had the same results as Jeff - sounds like a dodgy valve to me

Posted: Sun May 18, 2008 12:39 am
by whitegtipolo
it is the guy said he got it just after xmas from vag parts, will they replace it under warranty should have 12months on it from there??? :? really annoyed

Posted: Sun May 18, 2008 10:32 am
by Jeff GTi
not ideal for you mate, but least it looks like your going to get a brand new one from it after all, which is cool

Posted: Sun May 18, 2008 9:05 pm
by more-bhp
get your MBC on and not need J valve.....

fit your MBC in parallel and adjust until overboost/surging gone...

Posted: Sun May 18, 2008 9:18 pm
by whitegtipolo
more-bhp wrote:get your MBC on and not need J valve.....

fit your MBC in parallel and adjust until overboost/surging gone...
well i got an mbc now just need some t pieces, a new R32 couldnt get away from me today i was laughing at him! Got heat soak though after a while new intercooler is defo needed!!

Posted: Sun May 18, 2008 9:52 pm
by more-bhp
Getting those T pieces is a pain in the ar*e...

I got a whole box full of assorted sizes from Halfrauds..

Then you need loads of TINY jubilees..

R32...looool

I just spent hours and hours and hours getting my K04-001 on... what a job that is.... just NO room between engine and bulkhead...

Now boost is strong to red line and low down torque MUCH better.

Posted: Sun May 18, 2008 9:57 pm
by whitegtipolo
more-bhp wrote:Getting those T pieces is a pain in the ar*e...

I got a whole box full of assorted sizes from Halfrauds..

Then you need loads of TINY jubilees..

R32...looool

I just spent hours and hours and hours getting my K04-001 on... what a job that is.... just NO room between engine and bulkhead...

Now boost is strong to red line and low down torque MUCH better.
wat did you need 4 that conversion im up for that

Posted: Mon May 19, 2008 10:51 am
by more-bhp
you need K04-001, gaskets, washers, 4 bar FPR, new map..

If I get time I get 4 BAR FPR today and then start mapping..

The K04-001 isnt a massive power increase but there is more low down torque and the boost just keeps coming - doesnt run out of breath as quick as the K03.. I dont want to be changing clutches and fitting lsd and all that.. just want a bit more power...

So when you sprint to 60 in second there is still masses of boost.

Let me test so more first and I'll let you know how it goes...

Posted: Mon May 19, 2008 1:48 pm
by whitegtipolo
same ere cant be bothered with new diffs and that really till its a bit older and out of warranty etc , 8) sounds good let me know ya findings!

Posted: Tue May 20, 2008 12:35 am
by whitegtipolo
Getting pi55ed off with this valve situation i cleaned it out etc and thought lets try it again!!! so i reset ecu (disconnected battery etc) fit the valve went on a drive slow and let it learn a bit. Then it was working then not, and it went on like this for a while , then bam its like a new remap, its working mint rapid now lets hope its was just a glitch!! seems like the ecu didnt like it till it figured out wat to do with it! Ill see wat its like over the next few days etc might have just been sticking if not used for a while ! i hope so cos it feels well good spent £20 tonight beasting it about !!! :D

Posted: Tue May 20, 2008 8:29 am
by Jeff GTi
it definately provides a difference when working correctly eh

Posted: Tue May 20, 2008 8:37 am
by KennyPOLO_Gti
Might aswell purchase one of these! Wasnt to sure about gettin one after my problems with my old turbo but i might aswell! :roll: