1300 nearly broke down...random prob??

Chat about your MKI or MKII Polo (86 and 86F)
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steveo3002
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Joined: Sat Feb 12, 2005 1:46 pm

1300 nearly broke down...random prob??

Post by steveo3002 »

[:x] our 1300 f reg reg polo has started to play up big time

seems totaly random , it runs perfect the all of a sudden looses nearly all power and refuses to go,the only way to carry on is by redlining it and driving like a loon , then all of a sudden it will be sweet again

when its playin up , it doesnt seem to misfire, just sod all power and lots of kangerooing etc

ive just brought new leads and a coil [:s]

anyone any ideas...hall sender maybe
birmman
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Post by birmman »

Same happened to mine. Turned out to be a blocked fuel filter - the plastic inline one. Costs a quid to replace so worth checking!
steveo3002
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Post by steveo3002 »

mines new...cheers anyway
Gareth_GT_Hatch
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Location: Manchester Drives: '83 GL Classic

Post by Gareth_GT_Hatch »

yeah I was going to say sounds like fuel starvation. My derby had the same prob when I bought it. Fuel filter had been replaced but on inspection there was no petrol in it (but tank was full) So suspect was either a knackered fuel pump or blocked lines. Tried changing the pump first (easier job) and that sorted it. But if theres fuel in the filter then you can rule that out i suppose.
G340UTT
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carb icing

Post by G340UTT »

mine had the exact same prob...just didnt really do any kangarooing but everything else happen..

a few people said fuel starvation..so i check all the fuel lines and the filter and did the H.T leads and dizzy.....but still the same problem!!!

Eventually i found out it was carb icing which is a really problem with the pierburgs and most of the other carbed polos.......

took it to a garage and had the carb cleaned and tuned and the choke sorted out...it hasnt done it since but i have heard that the best way to solve to problem once and for all is to get a new weber!!!

it mite be more expensive but would be better in the long run!!


any help ???
Gareth_GT_Hatch
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Location: Manchester Drives: '83 GL Classic

Post by Gareth_GT_Hatch »

ah yes carb icing. When does the problem happen? on the motorway/driving at night etc...
steveo3002
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Post by steveo3002 »

mine has done it on a scalding hot day, and it also did it when hot started after standing

i'll have a look in the carb..see if its dirty
G340UTT
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carb icing

Post by G340UTT »

well the standard carbs on early volkswagens.....especially polos are naff!!

generally put in good service for the first 60,000 miles then just go down to pot!!


they are also unpredictable so its dosent supprise me that it happen on a hot day....even tho it mainly happens at night!!

its only a suggestion anyway check it and see......also if youve looked at you ignition components dizzy etc and they are ok and youve also checked your fuel lines, it must be sumin with ur carb!!

give it a clean and a reset and see

cheers
Tahrey1043
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Post by Tahrey1043 »

yeah i would have said to get someone to check out the pierburg, if your leads, fuel supply etc is all ok

dodgy tinplate nonsense :D
G340UTT
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carb prob

Post by G340UTT »

have you sorted it yet mate ???


did the carb advice help ??
steveo3002
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Post by steveo3002 »

well i cleaned the carb and fitted new ign leads and coil...as it was a random problem i cant really say if its fixed or not.....i'll leave it a few weeks till i decide its fixed :roll:

cheers for the help
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